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Dust Control System Helps
Sheet
Metal Fabricator Eliminate
Quality Control Problems
A Texas-based sheet metal fabricator was experiencing increased
part reject rates as a result of poor paint finish quality
caused by dust imbedded into the finished paint surface. Production
rates slowed due to re-working, or re-manufacturing rejected
parts. The company also experienced reduced per-piece profitability
resulting from increased overtime wages and facility maintenance
costs. The dust originated in an area where finish grinding
and sanding was done on welded metal parts prior to being
prepared for painting.

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The Airflow Systems Answer
The
company's paint booth was exhausted to the outside by equipment
which caused a strong negative pressure area within the plant.
This negative pressure caused a vacuum-like effect, drawing
dust into the paint booth. The company considered various
dust control equipment solutions, including constructing a
modular building in the facility for the grinding and sanding
area but was reluctant because of the cost. The company evaluated
a variety of in-plant dust control and air collection systems
including mechanical extractor arms, ambient systems, and
portable dust collector equipment. However, the local Airflow
Systems distributor presented a cost-effective alternative
to the companythe Airflow Systems DCB-2 Dust Control
Booth. The Airflow Systems DCB-2 is a totally self-contained
dust control filter booth, measuring 8'W x 8'D x 8'H. The
DCB-2 was able to enclose the grinding and sanding area without
the expense of a modular building. The Airflow Systems DCB-2
Dust Control Booth™ was powerful enough to overcome
the negative pressure within the plant and collect and clean
9000 cubic feet of shop air per minute.
Positive Proof of Dust Control
The Airflow Systems DCB-2 eliminated the dust migration problem
immediately. "The most important thing is our customers
are happyour reject rates are back to nearly zero,"
says the company's Production Supervisor. The company
was also able to realize significant cost savings following
the installation of the Airflow Systems DCB-2 equipment. "Without
the re-working and re-manufacturing we were able to eliminate
overtime wages, and with more efficient production we were
able to reduce per-piece manufacturing costs," said the
Production Supervisor. "These factors made an instant,
positive impact on our bottom line."
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